WE Report

Lessons Learned

Lesson Learned





By: Giacomo Bonomo

Report No.

6368

Discipline/Origin

Drilling
Own Experience

Well

Toppand East
35/11-5, 39/11-29S

Date created

2024/06/06
548 days ago

Project Phase

Operational
Project Phase

LL Type/Classification

Equipment
Negative

COSLPromoter

What happened in Reservoir section:
The BOP test tool could not be used, because one of the TJ was in conflict with the LPR. The TJ length considered in the drawings was shorter than the real length.

What Was Planned

All WH running tools need to be send out with correct space out pups. The drawings have been shared in advance with the rig to ensure no conflicts between BOP rams and tool joints

What Was Learned

Not possible to run the BOP test tool with the planned configuration. Need to source different pups for Gnomoria.

What Actions Are Required

Sourced extra PJ in IOT for Gnomoria well.

EDITOR


CLOSE LL (testing)





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