WE Report

Lessons Learned

Lesson Learned





By: Drilling Supervisor

Report No.

1427

Discipline/Origin

Drilling
Own Experience

Well

Oselvar
A-3 HT2

Date created

2021/04/20
1692 days ago

Project Phase

Operational
Project Phase

LL Type/Classification

Operational
Positive

Borgland Dolphin


What happened in P&A:
Optimised process as follows:
Lined up rig BOP Lower Kill line to rig choke manifold and autochoke.
Closed XOV and Master Valve on SFT. Opened PMV, AMV and ACV on HXT.
Pumped 5 m3, flushed any trapped gas below hanger to rig choke and poor-boy degasser.

What Was Planned

Flushing of possible gas trapped below tubing hanger after reverse circulating well to 1.35 SG brine.

What Was Learned

Efficient process.

What Actions Are Required

Repeat on next two wells.

EDITOR


CLOSE LL (testing)





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