WE Report

Lessons Learned

Lesson Learned





No user selected

Report No.

367

Discipline/Origin

Drilling
No origin

Well

Shrek
6507/5-9 S, 6507/5-9 A

Date created

2019/10/22
2237 days ago

Project Phase

Operational
Project Phase

LL Type/Classification

FIT/LOT
Positive

Deepsea Nordkapp


What happened in Reservoir section:
Performed FIT to 1.58 sg.

What Was Planned

Planned to do LOT below 9 5/8″ shoe.
(expected frac: 1.80 sg).

What Was Learned

Performed FIT instead due to limestone stringer just below the 9 5/8” shoe and risk of fracking formation above the reservoir.
Successful FIT.

What Actions Are Required

N/A

EDITOR


CLOSE LL (testing)





New Lesson Learned

You do not have permission to view this form.




\n\t\t

\n\t\t\t\n\t\t\t