WE Report

Lessons Learned

Lesson Learned





By: Drilling Supervisor

Report No.

1991

Discipline/Origin

Drilling
Own Experience

Well

Oselvar
A-3 HT2

Date created

2021/07/13
1608 days ago

Project Phase

Operational
Project Phase

LL Type/Classification

Operational
Positive

Borgland Dolphin


What happened in P&A:
Pulled pack off assembly free. Flow checked well. Pulled MPT with pack off assembly above BOP. Sheared circulation sub and circulated down string up 13 3/8″ x 20″ annulus through kill and choke lines. Flow rate 850- 600 lpm, 14 bar. No problems during circulation.

What Was Planned

Pull pack off assembly free with MPT. Pull pack off assembly and MPT above BOP and circulate 13 3/8″ x 20″ annulus to 1,75 sg mud prior to pull 13 3/8″ casing on separate run.

What Was Learned

Circulate annulus behind casing prior to pulling casing reduces risk of unbalanced fluid column causing backflow and potential gain signals.

What Actions Are Required

Use same set up on future operations.

EDITOR


CLOSE LL (testing)





New Lesson Learned

You do not have permission to view this form.




\n\t\t

\n\t\t\t\n\t\t\t