WE Report

Lessons Learned

Lessons Learned865


Operator Rig Discipline / Origin Project Phase Well Section Date What Happened

DNO
1222 – DNO

Borgland Dolphin Drilling
Experience Transfer Meeting
Operational A-1 H, A-2 H, A-3 HT2
Oselvar
Production section 06/05/2012 DONG handover documentation: Due to LWD tool failures on previous reservoir sections it was decided . . .

Include mud cooler in future reservoir sections with high temperature.
Karina Helle / Morten Laget


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DNO
1223 – DNO

Borgland Dolphin HSEQ
Experience Transfer Meeting
Operational A-1 H, A-2 H, A-3 HT2
Oselvar
Production section 06/05/2012 DONG handover documentation: Due to LWD tool failures on previous reservoir sections it was decided . . .

Include mud cooler in future reservoir sections with high temperature.
Karina Helle / Morten Laget


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DNO
1224 – DNO

Borgland Dolphin Drilling
Experience Transfer Meeting
Operational A-1 H, A-2 H, A-3 HT2
Oselvar
Production section 06/05/2012 DONG handover documentation: Due to LWD tool failures on previous reservoir sections it was decided . . .

Include mud cooler in future reservoir sections with high temperature. Alternative larger coolers on . . .
Karina Helle / Morten Laget


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DNO
1225 – DNO

Borgland Dolphin Drilling
Experience Transfer Meeting
Operational A-1 H, A-2 H, A-3 HT2
Oselvar
Production section 06/05/2012 DONG handover documentation: Due to the mud cooler the mud temperature was lower, this resulted in . . .

When planning to use a mud cooler consider effects on downhole mud temperature, weight and rheology . . .
Karina Helle / Morten Laget


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DNO
1226 – DNO

Borgland Dolphin Drilling
Experience Transfer Meeting
Operational A-1 H, A-2 H, A-3 HT2
Oselvar
Production section 06/05/2012 DONG handover documentation: The deactivation of the underreamer was not done on the bit trip due to . . .

Do not spend time deactivating unless circulating at the shoe for another reason (conditioning mud). . . .
Karina Helle / Morten Laget


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DNO
1227 – DNO

Borgland Dolphin Drilling
Experience Transfer Meeting
Operational A-1 H, A-2 H, A-3 HT2
Oselvar
Production section 05/05/2012 DONG handover documentation: After dropping the ball to activate the underreamer the string was . . .

As it looks like ball hangs up in string when not rotating, rotation should be initiated shortly . . .
Karina Helle / Morten Laget


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DNO
1221 – DNO

Borgland Dolphin Drilling
Experience Transfer Meeting
Operational A-1 H, A-2 H, A-3 HT2
Oselvar
Production section 22/04/2012 DONG handover documentation: During the scraping of the EZSV plug and Whipstock setting area the . . .

To avoid problems with hole instability during circulation (losses) the lowering of the mudweight . . .
Karina Helle


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DNO
1220 – DNO

Borgland Dolphin Drilling
Experience Transfer Meeting
Operational A-1 H, A-2 H, A-3 HT2
Oselvar
Production section 15/04/2012 DONG handover documentation: Started to get backflow when running the last 10 joints of blank pipe . . .

Change the OCG to prevent using excessive time on this in the future. Prepare a pit with heavy . . .
Karina Helle / Morten Laget


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DNO
1219 – DNO

Borgland Dolphin Drilling
Experience Transfer Meeting
Operational A-1 H, A-2 H, A-3 HT2
Oselvar
Production section 25/03/2012 DONG handover documentation: When running in with the seal assembly on MUT, the bullnose on the pipe . . .

In future run one more stand below MUT, so bullnose is stabbed into casing before picking up seal . . .
Karina Helle / Morten Laget


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DNO
1217 – DNO

Borgland Dolphin Drilling
Experience Transfer Meeting
Operational A-1 H, A-2 H, A-3 HT2
Oselvar
Production section 24/03/2012
DONG handover documentation:
When circulating prior to cementing initial pressure was 79 bar / . . .

Karina Helle / Morten Laget


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DNO
1218 – DNO

Borgland Dolphin Drilling
Experience Transfer Meeting
Operational A-1 H, A-2 H, A-3 HT2
Oselvar
Production section 24/03/2012 DONG handover documentation: The Odfjell CRTi (Casing Running Tool internal) was used to fill casing . . .

If using CRTi as a contingenct again is should be used together with auto filling shoe, this way . . .
Karina Helle / Morten Laget


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DNO
1216 – DNO

Borgland Dolphin Drilling
Experience Transfer Meeting
Operational A-1 H, A-2 H, A-3 HT2
Oselvar
Production section 11/03/2012 DONG handover documentation: While running the 13 3/8″ casing, the casing tong was not lowered all . . .

Karina Helle / Morten Laget


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DNO
1214 – DNO

Borgland Dolphin Drilling
Experience Transfer Meeting
Operational A-1 H, A-2 H, A-3 HT2
Oselvar
Production section 10/03/2012

Karina Helle / Morten Laget


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DNO
1215 – DNO

Borgland Dolphin Drilling
Experience Transfer Meeting
Operational A-1 H, A-2 H, A-3 HT2
Oselvar
Reservoir section 10/03/2012 DONG handover documentation: All joints for the 13 3/8″ casing came out with DL connections . . .

Karina Helle / Morten Laget


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DNO
1213 – DNO

Borgland Dolphin Drilling
Experience Transfer Meeting
Operational A-1 H, A-2 H, A-3 HT2
Oselvar
Production section 04/03/2012

Karina Helle / Morten Laget


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DNO
319 – DNO

Island Innovator Drilling Operational 6507/7-16 S
Canela
Production section Deliberately added 2 m pup after log interpretation showed potentially weak limestone stringer close . . .


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DNO
1303 – DNO

Island Innovator Operational 6507/7-16 S
Canela
Mye vær utfordringer Decemeber. HTI / Høy HS opp mot 7mtr Hs og 12 mtr bølger.


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DNO
1304 – DNO

Island Innovator Operational 6507/7-16 S
Canela
NPT Canela


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