WE Report

Lessons Learned

Lessons Learned865


Operator Rig Discipline / Origin Project Phase Well Section Date What Happened

DNO
8433 – DNO

Deepsea Yantai Drilling
Own Experience
Operational 35/10-13
Kjøttkake
Production section 15/03/2025 Not able to get BOP test – Burst seal on CHSART

Ole Marius Serigstad / Stig Seland


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DNO
8394 – DNO

Deepsea Yantai Drilling
Own Experience
Operational 35/10-13
Kjøttkake
Production section 07/03/2025 KOP set on ACST tool above 9 5/8” casing cut at ~1192 m to 1051 m (47 m inside 20” casing – shoe at . . .

Ole Marius Serigstad / Stig Seland


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PGNiG
8281 – PGNiG

Deepsea Yantai Drilling Operational 6501/10-1
Tomcat
Production section 15/02/2025 Installed brackets on OWS tong after derailing during 13 3/8″ job.

Drilling Engineer


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PGNiG
8282 – PGNiG

Deepsea Yantai Drilling Operational 6501/10-1
Tomcat
Production section 15/02/2025 Use an updated CRTi tool with active set function.

Drilling Engineer


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Wellesley
5844 – Wellesley

Deepsea Yantai Drilling Operational 35/10-10 A
Carmen
Production section 10/07/2023 Needed several trips with the tool up in the casing to cool it down.

Drilling Engineer / Morten Laget


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Wellesley
5157 – Wellesley

Deepsea Yantai Drilling
Own Experience
Operational 35/10-10S
Carmen
Production section 24/04/2023 It was done before the cementer got the change to da a pre-job check / install bypass baffle etc.

Drilling Engineer / Morten Laget


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Wellesley
5159 – Wellesley

Deepsea Yantai Drilling Operational 35/10-10S
Carmen
Production section 24/04/2023
Downtime due to reduced ROP after going to max ROP of 75 m/hr:
– Started with 30 m/hr
– Jumped up . . .

Drilling Engineer / Morten Laget


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Wellesley
5160 – Wellesley

Deepsea Yantai Drilling Operational 35/10-10S
Carmen
Production section 24/04/2023
Lube mud had 1.34 sg when taken up.
Needed to weight it down to ± 1.25 sg.
New lube mud for 12 . . .

Drilling Engineer / Morten Laget


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Wellesley
5115 – Wellesley

Deepsea Yantai Drilling Operational Eirik (OMV) Production section 30/03/2023 If we are leaning to one of the sides it is easy to hang up in something which can result in a . . .

Sander Schaathun / Morten Laget


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PGNiG
4946 – PGNiG

Deepsea Yantai Drilling
Experience Transfer Meeting
Operational 6608/1-1 S
Copernicus
Production section 03/11/2022
The gas readings for the 12 ¼” was done very well, and the correlation was quite good between the . . .

Richard Mollison



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PGNiG
4912 – PGNiG

Deepsea Yantai Drilling Operational 6608/1-1 S
Copernicus
Production section 20/09/2022 Time was spend circulating hole clean and even MW in/out.

Drilling Engineer / Morten Laget


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PGNiG
4845 – PGNiG

Deepsea Yantai Drilling Operational 6608/1-1 S
Copernicus
Production section 11/09/2022 Ran casing hanger through rotary and installed master bushing. Difficult to install due to short . . .

Drilling Engineer / Morten Laget


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Wellesley
2401 – Wellesley

Borgland Dolphin Drilling
Own Experience
Operational 36/1-4
Hemispheres
Production section 30/12/2021 ALL mud skips was put on the same boat, effectively removing any hope for recieving backload on said . . .

Drilling Engineer / Morten Laget


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INEOS
2316 – INEOS

Borgland Dolphin Drilling
Own Experience
Operational 6306/3-1 S
Fat Canyon
Production section 09/12/2021 Extremeley slow drilling. At worst it was down to 1-2m/hr. At best it was 9-12m/hr.

Steinar Aarnes / Morten Laget


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INEOS
2317 – INEOS

Borgland Dolphin Drilling
Own Experience
Operational 6306/3-1 S
Fat Canyon
Production section 09/12/2021
Extremely slow progress ranging from 1-10m/hr.
Likely due to sweeling/stickyness of clay due to use . . .

Steinar Aarnes / Morten Laget


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INEOS
2318 – INEOS

Borgland Dolphin Drilling
Own Experience
Operational 6306/3-1 S
Fat Canyon
Production section 09/12/2021
The used 9 5/8″ casing was run quite smoothly. Not a single joint rejected, and Frank’s tongs . . .

Steinar Aarnes / Morten Laget


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INEOS
2320 – INEOS

Borgland Dolphin Drilling
Own Experience
Operational 6306/3-1 S
Fat Canyon
Production section 09/12/2021
Managed to barely land the casing in very sticky clay.

Since the mainbore 9 5/8″ casing became . . .

Steinar Aarnes / Morten Laget


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INEOS
2303 – INEOS

Borgland Dolphin Logistics
Own Experience
Operational 6306/3-1 S
Fat Canyon
Production section 14/11/2021 The BHA was sent from Stavanger to Kristiansund, and after screening the loadout list from . . .

Drilling Engineer / Morten Laget


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INEOS
2302 – INEOS

Borgland Dolphin Drilling
Own Experience
Operational 6306/3-1 S
Fat Canyon
Production section 10/11/2021 Went down with 9 5/8″ cutters and cut the casing, observed 75 bar pressure drop and torque drop to . . .

Drilling Engineer / Morten Laget


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INEOS
2273 – INEOS

Borgland Dolphin Logistics
Own Experience
Operational 6306/3-1 S
Fat Canyon
Production section 05/11/2021 During operation drilling did go slower than expected and way too often the boats has to go to the . . .

Drilling Engineer / Morten Laget


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