WE Report

Lessons Learned

Lessons Learned865


Operator Rig Discipline / Origin Project Phase Well Section Date What Happened

Wellesley
208 – Wellesley

Transocean Arctic Drilling Operational 35/12-6 S
Kallåsen
Production section 07/02/2019 The Halliburton BSS “skip & ship” system worked very well. There was no problem handling60 m/hr . . .


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Wellesley
209 – Wellesley

Transocean Arctic Drilling Operational 35/12-6 S
Kallåsen
Production section 07/02/2019


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Wellesley
210 – Wellesley

Transocean Arctic Drilling Operational 35/12-6 S
Kallåsen
Production section 07/02/2019 Problems experienced with poor quality of pre-doped connections. Remains of rusty water and storage . . .


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Wellesley
211 – Wellesley

Transocean Arctic Drilling Operational 35/12-6 S
Kallåsen
Production section 07/02/2019 The pump strokes and volume pumped (from pit sensors) matched very well from 0-83 m3 mud pumped . . .


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Wellesley
212 – Wellesley

Transocean Arctic Drilling Operational 35/12-6 S
Kallåsen
Production section 07/02/2019 All 3 wiper plug shears & burst were clearly seen during this cement job; bottom plug shear, top . . .


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Wellesley
213 – Wellesley

Transocean Arctic Drilling Operational 35/12-6 S
Kallåsen
Production section 07/02/2019 Trip sheet from Geoservice and Transocean has shown different numbers. In addition, gains have been . . .


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Wellesley
183 – Wellesley

Transocean Arctic Drilling Operational 35/12-7
Serin
Production section 05/02/2019 Drilled stab-in float collar in only 50 minutes, but used 3.5 hrs to drill shoe, which is more than . . .


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Wellesley
184 – Wellesley

Transocean Arctic Drilling Operational 35/12-7
Serin
Production section 05/02/2019 Had to lay out several joints due to missing threads on top of pin ends, (9 5/8″, #53.3, P-110, . . .


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Wellesley
201 – Wellesley

Transocean Arctic Drilling Operational 35/12-6 S
Kallåsen
Production section 05/02/2019 Tried to shear OBM mud in pits before drilling the 12 1/4″ section. At this time the well and all . . .


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Wellesley
204 – Wellesley

Transocean Arctic Drilling Operational 35/12-6 S
Kallåsen
Production section 05/02/2019 Coating from 9 5/8″ casing blocked dices on Franks casing tong (upper jaws). Had to frequently clean . . .


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Wellesley
205 – Wellesley

Transocean Arctic Drilling Operational 35/12-6 S
Kallåsen
Production section 05/02/2019 Double float valves in shoe failed at around 900 m, still inside 13 3/8″ casing. Mud flowed back . . .


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DNO
316 – DNO

Island Innovator Operational 6507/7-16 S
Canela
Production section 07/01/2019 Drilled section with planned mud and mud weight without problems with cavings. Cavaings identified . . .


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DNO
317 – DNO

Island Innovator Drilling Operational 6507/7-16 S
Canela
Production section 07/01/2019 Drilled section with planned mud and mud weight without problems with cavings. Cavaings identified . . .


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DNO
320 – DNO

Island Innovator Drilling Operational 6507/7-16 S
Canela
Production section 07/01/2019 Great care taken breaking circulation at casing TD/washing down to land off. Used 100 lpm steps, . . .


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DNO
321 – DNO

Island Innovator Drilling Operational 6507/7-16 S
Canela
Production section 07/01/2019 High values of LOT/FIT expected; 1.95 sg EMW. Value of ESD measured by LWD tool ahead of FIT was . . .


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DNO
1222 – DNO

Borgland Dolphin Drilling
Experience Transfer Meeting
Operational A-1 H, A-2 H, A-3 HT2
Oselvar
Production section 06/05/2012 DONG handover documentation: Due to LWD tool failures on previous reservoir sections it was decided . . .

Include mud cooler in future reservoir sections with high temperature.
Karina Helle / Morten Laget


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DNO
1223 – DNO

Borgland Dolphin HSEQ
Experience Transfer Meeting
Operational A-1 H, A-2 H, A-3 HT2
Oselvar
Production section 06/05/2012 DONG handover documentation: Due to LWD tool failures on previous reservoir sections it was decided . . .

Include mud cooler in future reservoir sections with high temperature.
Karina Helle / Morten Laget


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DNO
1224 – DNO

Borgland Dolphin Drilling
Experience Transfer Meeting
Operational A-1 H, A-2 H, A-3 HT2
Oselvar
Production section 06/05/2012 DONG handover documentation: Due to LWD tool failures on previous reservoir sections it was decided . . .

Include mud cooler in future reservoir sections with high temperature. Alternative larger coolers on . . .
Karina Helle / Morten Laget


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DNO
1225 – DNO

Borgland Dolphin Drilling
Experience Transfer Meeting
Operational A-1 H, A-2 H, A-3 HT2
Oselvar
Production section 06/05/2012 DONG handover documentation: Due to the mud cooler the mud temperature was lower, this resulted in . . .

When planning to use a mud cooler consider effects on downhole mud temperature, weight and rheology . . .
Karina Helle / Morten Laget


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DNO
1226 – DNO

Borgland Dolphin Drilling
Experience Transfer Meeting
Operational A-1 H, A-2 H, A-3 HT2
Oselvar
Production section 06/05/2012 DONG handover documentation: The deactivation of the underreamer was not done on the bit trip due to . . .

Do not spend time deactivating unless circulating at the shoe for another reason (conditioning mud). . . .
Karina Helle / Morten Laget


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