WE Report

Lessons Learned

Lessons Learned865


Operator Rig Discipline / Origin Project Phase Well Section Date What Happened

Wellesley
464 – Wellesley

Borgland Dolphin Drilling Operational 6204/11-3
Schweinsteiger
Top hole 27/08/2020 No fill on 36″ hole wiper trip. Ran 30″ conductor, found 1m fill on bottom. Washed to bottom, picked . . .

Drilling Supervisor


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Wellesley
465 – Wellesley

Borgland Dolphin Drilling Operational 6204/11-3
Schweinsteiger
Top hole 27/08/2020 Good suggestion from Dolphin not to do this as in past fibreglass tubing has broken due to vibration . . .

Drilling Supervisor


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Wellesley
462 – Wellesley

Borgland Dolphin Drilling Planning 6204/11-3
Schweinsteiger
26/08/2020 To low budget time on rig move

Morten Laget


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Wellesley
463 – Wellesley

Borgland Dolphin Drilling Operational 6204/11-3
Schweinsteiger
Top hole 26/08/2020
Bentonite loaded onto rig in fjord but problems transferring from silos to surge tank in pit room . . .

admin


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Wellesley
450 – Wellesley

Borgland Dolphin Drilling Planning 6204/11-3
Schweinsteiger
N/A 12/08/2020 Slow progress and no clear recommendations.

Morten Laget


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Wellesley
233 – Wellesley

Transocean Arctic Drilling Operational 35/11-21 S
Grosbeak West
Surface section 16/06/2020 Several joints had to be broken out and made up again due to difficulties with centralizing joints . . .


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Wellesley
234 – Wellesley

Transocean Arctic Drilling Operational 35/11-21 S
Grosbeak West
Production section 16/06/2020 Good experience M/U 9 5/8″ VAM21 CWD2 joint with drilling bails rather than longer casing bails. . . .


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Wellesley
235 – Wellesley

Transocean Arctic Drilling Operational 35/11-21 S
Grosbeak West
Reservoir section 16/06/2020 Dropped 2 15/16″ drift to check 5 1/2″ DP/HWDP prior to coring (coring ball 1 1/4″). The drift was . . .


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Wellesley
236 – Wellesley

Transocean Arctic Drilling Operational 35/11-21 S
Grosbeak West
Reservoir section 16/06/2020 720 litres of crude oil was left in bottom of well after MDT sampling on wireline. The MDT run was 2 . . .


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Wellesley
243 – Wellesley

Transocean Arctic Drilling Operational 35/11-21 A
Grosbeak
Intermediate section 16/06/2020 The remote operated lo-torq valve was installed with an elbow between side inlet and lo-torq, while . . .


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Wellesley
244 – Wellesley

Transocean Arctic Drilling Operational 35/11-21 A
Grosbeak
Intermediate section 16/06/2020 Making up cmt. Stand into landing string prior to landing 9 5/8″ casing was done by use of chain . . .


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Wellesley
245 – Wellesley

Transocean Arctic Drilling Operational 35/11-21 A
Grosbeak
Reservoir section 16/06/2020 There were 5 wireline drums on the rig during wireline logging and logging on DP. The operations . . .


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Wellesley
246 – Wellesley

Transocean Arctic Drilling Operational 35/11-21 A
Grosbeak
Reservoir section 16/06/2020 Inner bushing with cut-out for wireline was not mobilized for this wireline conveyed logging job. A . . .


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Wellesley
247 – Wellesley

Transocean Arctic Drilling Operational 35/11-21 A
Grosbeak
Reservoir section 16/06/2020 During sampling it was found out that the exit point was not consistent to be on top of the FTWT . . .


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Wellesley
248 – Wellesley

Transocean Arctic Drilling Operational 35/11-21 A
Grosbeak
Reservoir section 16/06/2020 Max flowrate for extracting formation fluid with the FTWT tool was said to be 6-7 lpm. During this . . .


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Wellesley
249 – Wellesley

Transocean Arctic Drilling Operational 35/11-21 A
Grosbeak
Reservoir section 16/06/2020 N/A


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Wellesley
250 – Wellesley

Transocean Arctic Drilling Operational 35/11-21 A
Grosbeak
P&A 16/06/2020 N/A


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Wellesley
251 – Wellesley

Transocean Arctic Drilling Operational 35/11-21 A
Grosbeak
P&A 16/06/2020 N/A


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Wellesley
252 – Wellesley

Transocean Arctic Drilling Operational 35/4-2
Songesand
Top hole 16/06/2020 When cement was in place and 10 MT weight was slacked off conductor to set it on bottom, noticed the . . .


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Wellesley
253 – Wellesley

Transocean Arctic Drilling Operational 35/4-2
Songesand
Surface section 16/06/2020 The back-up 18 3/4″ wellhead assembly was sent out incomplete, without running tool, 9 m DP mandrel, . . .


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